Monday, 1 July 2013

22. BSA A10 Finished / Modifications & Repairs

Having discovered that my A10 super rocket was seriously leaking oil, I started to think about what could be causing it. One thing was certain, this was no leaking gasket, this was serious. It occurred to me that it could be only one of two possibilities.

1. The oil pump was not returning the oil to the tank, allowing it to build up in the sump and then be forced out of the breather by crankcase compression.

2. The whole problem could be caused by crankcase compression, after all I had not replaced the pistons or valves as they all looked fairly good to me.

I decided to look at the oil pump first. I removed the right side exhaust and timing cover, along with the tacho drive and took a look at the oil pump. But with no way of measuring it's output a visual check was all that was possible and it looked OK. I then noticed that I had only put a gasket under the main body and had not put one under the tacho drive end of the pump. A quick phone call to Lightning spares confirmed that this could be the source of the problem as without a gasket on both ends, the pump cannot seat properly and sits at an angle to the crankcase. Great, I thought. I fitted the small round gasket to the tacho end of the pump and put the bike back together. Unfortunately the result was the same with large amounts of oil being blown out of the breather.

After a great deal of thought, I came to the conclusion that without the correct test equipment, I might never find the source of the problem and so I took the expensive decision to take the bike back to SRM another 340 mile round trip.

Having taken the bike to SRM in the trailer (which I left there) they got on with the investigation and removed the oil pump and put it on a test rig. The tests proved that the pump emptied the test tank in 14 seconds but took 42 seconds to refill the tank. So my sump was slowly filling up with oil. I said OK to a new oil pump, which they fitted and the oil now returned to the tank correctly. However this was not the end of the problem. Oil was still blowing out of the breather, although nothing like as bad as before.

I gave them the go-ahead to strip the engine and investigate and the end result was that my visual inspection had not been enough to ensure that the engine was fit for the rebuild. In fact it revealed that the engine needed new pistons and rings, re-sleeving of the barrels, new valves and guides, new valve seats and valve springs. Expensive! but there was absolutely no point in reassembling the engine with the old parts in it, so I said "go ahead". A week later I collected the bike and trailer and it ran beautifully with no oil leaks.

Time for its MOT which was just around the corner at a bike shop called "Street Machine" and it passed, although I did have some difficulty with the gears getting it there. Once MOT'd I got the new free tax disc and at last I was on the road.

The first ride was a mixture of total exhilaration mixed with disappointment. The bike handled and accelerated brilliantly. The disappointment was the gear change. No matter how I tried I could not get it to change down once I had changed up the gears. This did not stop me taking the bike to its first show at Thorsby Park where I showed it alongside the scooter (Mods & Rockers) and where it got lots of attention although no win. In fact the scooter won!


After the show I took the bike back to the workshop and tried it again up the road. But the gears were still impossible to select when changing down. I suppose that at this point I became lazy and instead of stripping the gearbox again, I decided to make the trip again to SRM. If only I had asked them last time to road test the bike before collecting it. But I didn't.

So for the third time I took it back to Wales again and this time I said "check everything" "make sure it is 100% before I fetch it back" and they did. The gearbox problem turned out to be an "indexing problem" which they fixed without removing the box and the bike road tested perfectly.

I collected it and brought it home, just in time to attend the Rockingham show, at which it came second out of 120 bikes.

I then took it to the Belper steam rally, where there are no prizes, but it got lots of attention and was photographed for use by a company who make metal wall signs. See:
http://www.ebay.com.au/itm/BSA-A10-SUPER-ROCKET-MOTORCYCLE-METAL-SIGN-/400515757847?pt=UK_CarParts_Vehicles_Manuals_Litterature_ET&hash=item5d40997717

Two more shows followed: The Grantham Show, where the bike won a trophy for "Best Motor Cycle" (and the scooter won "Best Scooter") and Yesterday, back at Thorsby Park, where the scooter won best 60's bike and the BSA Super Rocket won "BIKE OF THE SHOW"
And that is the end of the blog, unless you want more? If you do click "Newer Post" and keep reading.

I would like to express my sincere thanks to Lightning Spares, of Birmingham and SRM Engineering of Aberystwyth, without who's help this project would not have been completed.

My next project: 1954 BSA Bantam.

MODIFICATIONS & REPAIRS
This section has been added after the renovation and keeps you up to date with any changes or problems I may have with the BSA A10 Super Rocket.

TWIN LEADING SHOE FRONT BRAKE.
After taking the BSA A10 to several rallies and going on a few road runs, one thing was very apparent. Whilst the performance was great, the brakes were definitely 1961 and in order to come to a stop in a sensible distance, it was necessary to use both the front and rear brake and change down through all the gears and in modern traffic, this just wasn't good enough.

So I started looking at possible front brake modifications and it didn't take me long to realise that what I needed was a "Twin Leading Shoe" front brake.

This first picture shows the original brake. Although it was totally overhauled and was one of the later full width hubs, its braking ability was still extremely limited.














So after searching the Internet, I found this one for sale on EBay. As you can see, it's a reproduction one, but nicely made. Unfortunately, apart from the outer rim, the rest of the back plate is a rough sand casting and all of the lever system was galvanised. So two jobs now faced me. Firstly strip off all the lever system and send all of the parts off for chrome plating. Secondly, start the long job of polishing the back plate up to the standard of the rest of my bike.

The good news was that it came with a nice new set of brake shoes and the new brake fits in my existing brake drum nicely and the axle passes through the centre hole perfectly.

However trying the wheel back in place with the new brake fitted revealed two small modifications necessary. Firstly, with the retaining nut on the axle, holding the plate in place. It would not fit between the front forks and I couldn't get the end caps on the bottom of the forks. To cure this I had to put the retaining nut in the lathe and turn it down to half its thickness. Now the wheel and hub fit between the forks.

The next problem was that the lug on the inside of the right fork, that stops the back plate rotating when the brake is applied, would not fit between the slot on the back plate. This was only about 1mm too tight so I removed a little metal from the back plate slot with a Dremel fitted with a rotary sanding disc. The wheel and hub now fit perfectly.

Polishing the back plate took a very long time, as the surface is quite complicated with lots of small nooks and crannies. I found some very useful bits for my Dremel, which consisted of some small green rubber tipped bits that were impregnated with a fine abrasive. These were great for getting into difficult places but wore out very quickly and I think I got through about 15 of them before I was totally happy with the finish.

Now all of the bits arrived back from the chrome platers and they look much better. So after re-assembling the back plate, the wheel with its new hub could be fixed into place between the forks. and this presented another problem. The mudguard stays now did not fit. The front one hit the air intake and the rear one hit the actuating mechanism. I was faced with a decision: make some bent stays or reposition them. I decided to go for the latter.

The front stays were easy. The aluminium plates that I had made to fix the front stay to the fork end cap had an offset lug on it. By swapping the left plate for the right one I offset the front stays sufficient to clear the air intake.


The rear one was not so easy. I decided to take the mudguard to my friend at Unit Two Services, Ilkeston, and ask him to cut off the rear lugs and reposition them as my welding skills are poor and he's brilliant at welding stainless steel. So I marked to mudguard where I wanted the lugs, higher up the mudguard and left him to it. He cut them off and re-welded them back on perfectly, so all I needed to do was re-polish the mudguard and refit it.

Obviously I did both sides of the mudguard so that they would look symmetrical and now the stay clears the mechanism perfectly.

The final thing to do was adjust the brake and then road test it.

Wow!! just a touch on the brake lever stops the bike dead and I'm happy with the way it looks too.







Saturday, 11 May 2013

21. BSA A10 Ain't that a kick in the head!

Today should be the day that my1961  BSA A10 Super Rocket comes to life. All I have to do is fit the carburetor, the fuel tank and the fuel pipes and the engine should run!

I stripped the carburetor and polished the casing then blew out all of the airways  with compressed air, fitted all new jets and gaskets and reassembled it. 


I then fitted it onto the inlet manifold with a new stainless steel drip plate and  a nice new long bell mouth.

The fuel tank dropped on and secured in place with the central nut and rubber bung cover and the securing strap underneath and on went the new braided stainless steel fuel pipes.

With fuel in the tank it is time for the first kick. I kicked - nothing!, I kicked again - nothing! I kicked and kicked and kicked but apart from a very occasional backfire, it showed no signs of life at all. What a huge disappointment.

I took out the plugs and fitted new plugs and new HT leads, I checked the spark and there was one, if a little weak. I checked the fuel was getting through. My thought was that I must have got the timing wrong, although I was very careful when I set it. So I stripped the timing side down again and re-timed the ignition. Reassemble the engine and tried again. NOTHING.

There only one thing for it, I needed an expert. I have learnt over the years that the secret of good D.I.Y. was to know when to stop and I had reached that point. After scouring the Internet there seemed to be only one good choice. A company called SRM Engineering in Aberystwyth, Wales. I spoke to them over the phone and they were very helpful, so I arranged to take the bike the 170 miles and have it with them first thing in the morning so that they could have a full day on it.

So I left home at 05:00am and got the bike to them by the time they opened. I then had to occupy myself in Aberystwyth for the day (Not easy). However at 400pm I got a call to say that it was running, and rushed back to see for my self. Sure enough it was running and sounded great. So what was the problem? If you remember earlier in my blog, when I was stripping the bike, I had a problem removing the magneto and eventually I knocked it out and it hit the floor. Well it is possible that this was the cause because the problem was a bent armature in the magneto. So slight that with the plugs out, you got a spark. But with them in the magneto could not work as the armature was just touching the windings. I am not certain that the drop I gave it caused this, as the reason I stripped it in the first place was because I could never get it to run correctly. But anyway it now runs.

Geoff, the mechanic, said "Oh by the way, you've got a bit of an oil leak"   I thought "never mind I can fix that when I get back". So back home I went another 170 miles but feeling good.

Back in the workshop, I proceeded to do the wiring on the bike with a new loom and fit the speedo and tacho. It was obvious when I started the bike that it wasn't charging and the tacho wasn't working.

I took the tacho and speedo to a local expert called Russel Smalley, who took one look at the tacho and said "what bike have you got?" I told him "A10 Super Rocket". "and where are you driving it from?" I said "The oil pump drive". He said "It will never work!" It turns out the the tacho I bought was off a BSA 500 Gold Star. That engine turns the tacho clockwise. The A10 turns the tacho anti-clockwise. He proved it by putting it on a machine and turning it the right way and sure enough it worked. I asked could he do anything with it and he informed me that he could machine the mechanism and add another gear to make it turn in the right direction. Great.

Now the speedo. "What bike is this off?" he said. Again I answered "my A10, I took that one off the bike my self". "No it isn't, it's off a Triumph".  OMG again he proved it by showing me that the gearing was wrong for the BSA and that it did not show the correct speed. Someone must have swapped it at some point in the bikes 50 year life. He told me that he would have to fit a complete new mechanism and I said OK and left them both with him. A week later I had them back and they looked brand new and worked perfect.



 Back to the electrics. The problem turned out to be the old regulator, so I bought a new electronic one and hid it inside the old mechanical regulator housing, inside the tool box. Hey presto! it now charges.


With the electrics working and the clocks, time for my first ride up and down the car park outside my factory unit.

WOW! it is fast and sounds magnificent. But just when I was feeling really good, I looked at the ground and saw a huge oil trail following my path up and down the car park.

Close inspection showed that all of the oil in the oil tank had gone in four short trips.

More on this in the next blog


"Under Pressure"

 I would love to read your comments on this blog. If you would like to make some please click "Subscribe to: Post Comments (Atom)" at the bottom of this page. If you would like to be automatically informed when a new episode is posted then please tick the "Join this site" box at the bottom of the page. Thanks for reading. Kevin

 Copyright K. Hopcroft  11.05.13 All rights reserved
 You can contact me on: hopcroftscoot@gmail.com

My Other Blogs:

1961 Ariel Arrow Super Sport Motorcycle :
http://60sclassicmotorbikes.blogspot.co.uk/2014/01/1961-aerial-golden-arrow-restoration.html

Miniature Land Rover Defender:
http://miniaturelandrover.blogspot.co.uk/2016/02/1-miniature-land-rover-defender-idea.html?view=timeslide

1971 VW Karman Ghia Convertible Car:
http://karmannghiarestoration.blogspot.co.uk/2017/03/1-karmann-ghia-retoration-project.html

Motorcycle Trailers / Caravans:
http://motorcycletrailersandcaravans.blogspot.co.uk/2018/01/1-motorcycle-trailers-problem.html

Friday, 22 March 2013

20. BSA A10 Oil be seeing you

At last it's time to put some oil in the bike and that means fitting all the oil associated parts. First the rocker return oil pipe. Not quite as easy as I expected. The banjo bolts fitted easily along with the fibre washers each side of the union. But the pipe comes straight and has to be bent to follow the path it has to take. It didn't take long to figure out the route but the pipe is quite hard to bend and I did not want to kink it, so I found pieces of round wood to bend it around. It went up from the rocker box, under the frame from left to right an then followed the frame back and down towards the oil tank position.

Next was the oil tank itself. I had bought the mounting kits and offered the tank into place only to find that there was nowhere to bolt the bottom fixing to. Having studied the original stripping photos (Shown here) I soon discovered that the previous owner had made a home made bracket bolting the oil tank directly to the battery tray. This was very wrong as the tank should be rubber mounted to prevent it from fracturing due to vibration. I studied the parts book and found that there was a special loop bracket that fitted on the battery tray mountings with two captive nuts on it that replaced the right hand battery tray mounting nuts and I just didn't have this part. A quick call to Lightning Spares and Brian had a nice new bracket on its way to me and once it arrived it fit beautifully.

Now I could mount the oil tank and the oil send and return pipes along with a new banjo fitting that connects to the rocker return pipe. I had quite a bit of confusion as to whether to fit an oil none return valve or not. Lots of mixed reports on this on the Internet. Wet sumping, where the oil tank empties itself into the sump when the bike is not used for a period of time is a very common problem. But the none return valve is said to cause cavitation and stop oil reaching the big ends etc. on sustained long journeys. What to do? In the end I made a decision, this bike will not do long journeys and will spend most of its life in my workshop or at vintage shows. Estimated mileage per year about 50 miles maximum. So I fitted the valve.

Time to pour some oil in. I took advice from Lightning Spares again and bought standard 20/50 motor oil. I put a quarter of a pint directly into the rocket box and then filled the tank to the correct level. Next was to put oil in the gear box and the primary chain drive case (just enough for the chain to dip into it).

That done, all I need to do is connect the fuel and try starting it!

Next blog: The first kick!!!

 I would love to read your comments on this blog. If you would like to make some please click "Subscribe to: Post Comments (Atom)" at the bottom of this page. If you would like to be automatically informed when a new episode is posted then please tick the "Join this site" box at the bottom of the page. Thanks for reading. Kevin


 Copyright K. Hopcroft  22.03.13 All rights reserved
 You can contact me on: hopcroftscoot@gmail.com

My Other Blogs:

1961 Ariel Arrow Super Sport Motorcycle :
http://60sclassicmotorbikes.blogspot.co.uk/2014/01/1961-aerial-golden-arrow-restoration.html

Miniature Land Rover Defender:
http://miniaturelandrover.blogspot.co.uk/2016/02/1-miniature-land-rover-defender-idea.html?view=timeslide

1971 VW Karman Ghia Convertible Car:
http://karmannghiarestoration.blogspot.co.uk/2017/03/1-karmann-ghia-retoration-project.html

Motorcycle Trailers / Caravans:
http://motorcycletrailersandcaravans.blogspot.co.uk/2018/01/1-motorcycle-trailers-problem.html

Sunday, 10 March 2013

19. BSA A10 Exhausted Time To Sit Down

The next stage on the renovation of my BSA A10 Super Rocket is to fit the exhaust. All of the original exhaust parts were pitted and dented in fact the only parts worth keeping were the two finned heat sinks. So I re-threaded them to take 8mm Allen key stainless steel bolts and polished them as best I could between the fins and that was the total of the old exhaust renovation. The old exhaust pipes and silencers I put on eBay and despite a very honest description and photos of all the dents and damage, they sold for excellent prices. So that went a little way towards the cost of the new exhaust system.

I then decided to buy a pair of stainless steel swept exhaust pipes off eBay and new Rocket Gold Star silencers from Lightning Spares. Until I spoke to them I had not noticed the difference. Super Rocket silencers are the same cigar shape at both ends. Rocket Gold Star silencers taper towards the front of the bike. You live and learn! The picture above shows the original exhaust.

I offered the new pipes in place along with the new silencers and it was immediately apparent that I would need a couple of spacers, where the silencers bolt to the frame to hold the new front pipes away from the engine casing, so I set about making some aluminium spacers and also replaced the rear foot rests, which hold the silencers in place, with new polished stainless bolts. No need for the foot rests as I'm putting a single seat on it.

At the front of the new exhaust pipes were two welded on small tubes set at right angles to the exhaust pipes. I soon figured out that, as these new swept pipes did not follow the line of the frame, they could not be bolted to the frame to secure them. The answer was to fit a bar between the two pipes and through these tubes to secure them to each other. But what to use? I found that the inside diameter of the small tubes was 10mm and that started me thinking about what I already had. My firm uses a lot of 10mm stainless steel threaded rod so I measured the required length and cut a piece off. Next I measured how much thread I needed either side of the fixing tubes and marked that. This left the long bit in between the two threads. My first thought was to cover it with a tube, but then a friend suggested that it would be better to simply put the rod in my lathe and turn the threads off, leaving a smooth bar in the middle. Brilliant!. Having done that 10mm nuts were acquired and a chamfer turned on all of the nuts so that they could bottom on the fixing tubes without hitting the exhaust pipes. All polished and fitted it looked a treat and allowed me to adjust the distance between the two pipes to ensure crankcase clearance.

The standard BSA exhaust clamps just did not look good enough, so I pulled out a card that I had collected at the Newark Classic Bike Show, in January, and phoned the man. He had exactly what I wanted beautiful 42mm stainless Allen Key clamps ready polished.

Now just a case of fitting it all. It originally came as a surprise, when I first stripped the bike, to find that there was no secure fixing for the exhaust pipes into the cylinder head. To ensure that I did not get leaks I put a liberal coating of high temperature silicon sealant around the pipes before fitting them and behind the finned heat sinks. All then bolted in place and it looks just great.

Just as I finished fitting the exhaust, my seat brackets arrived. I had been waiting for them for weeks. Having decided to fit a single seat, I had seen the one I wanted on a photo on the web and after making enquiries, I found out that it was originally off a BSA Lightning. Finding a stockist on the web was not too difficult, but when it arrived it was obvious that none of the A10 fixing points lined up. This meant that I had to design a seat bracket system from scratch. So I set about making one out of aluminium. See picture on the right.

I also had to re-drill the front  seat mounting fork to bring it nearer to the A10 frame mounting. That done I had sent the aluminium bracket off to have a proper and stronger Stainless one  made.

Now at last I could try it in place and offer the seat onto the bike. I fitted the new bracket into the seat and the new support bridge piece onto the mudguard and tried it in place. It fitted but the seat was a little off to one side. Not surprising really as aluminium is so easy to bend . But it only required one hole being re drilled on the bracket under the seat and it fitted perfectly.

It had occurred to me that I deeded to remove the seat easily to get at the battery. So the bracket was designed with the two studs sticking down, which passed through the new mudguard seat support bracket. I then turned two large aluminium knurled knobs to fit the studs and hold the seat in place, putting two rubber washers between the knobs and the bracket to stop them vibrating off.



Now, with the Gold Star petrol tank just sitting in place, the seat could finally be fitted and a first idea of what the bike will finally look like could be seen. What do you think?

 I would love to read your comments on this blog. If you would like to make some please click "Subscribe to: Post Comments (Atom)" at the bottom of this page. If you would like to be automatically informed when a new episode is posted then please tick the "Join this site" box at the bottom of the page. Thanks for reading. Kevin

 Copyright K. Hopcroft  10.03.13 All rights reserved
 You can contact me on: hopcroftscoot@gmail.com

My Other Blogs:

1961 Ariel Arrow Super Sport Motorcycle :
http://60sclassicmotorbikes.blogspot.co.uk/2014/01/1961-aerial-golden-arrow-restoration.html

Miniature Land Rover Defender:
http://miniaturelandrover.blogspot.co.uk/2016/02/1-miniature-land-rover-defender-idea.html?view=timeslide

1971 VW Karman Ghia Convertible Car:
http://karmannghiarestoration.blogspot.co.uk/2017/03/1-karmann-ghia-retoration-project.html

Motorcycle Trailers / Caravans:
http://motorcycletrailersandcaravans.blogspot.co.uk/2018/01/1-motorcycle-trailers-problem.html

Sunday, 17 February 2013

18. BSA A10 The Generation Game


The continuing saga of the BSA A10 Super Rocket rebuild. Time to look at the dynamo, I had removed the dynamo back in February 2012 and it had sat in a draw in my workshop ever since. Stripping it was not too difficult but the inside revealed the usual signs of old age along with large quantities of oil. I can only assume that with the bike standing still for so long, the oil tank had slowly emptied itself into the sump (known as "wet sumping") and then when eventually the previous owner had got the bike running the oil was forced past the old oil seals and into the dynamo. Needless to say the coil was soaked along with the armature and the brush gear. I stripped it down completely and inspected each part and then contacted a chap who advertises himself in the BSA Star magazine as "Dynamo Dynamo". He was extremely helpful and advised me on what parts I needed and the costs. Basically I replaced everything except the armature and the body.

Once I received the parts, I selected all of the items that could be seen on the outside, including the main body and the brush gear cover and sent them away for chroming. I then set about polishing the aluminium end caps and cleaning up everything else.

Sometime later the chromed parts arrived back and I set about reassembling the dynamo. The idea was first to do a "dry build", just to see that everything fitted and that nothing was missing. This turned out to be a good idea, as as soon as the coil and the armature were bolted in place, it was obvious that the armature would not turn and was fouling on the coil. I spoke to the Dynamo man and he informed me that you needed a special tool to tighten the coil in place, but that also sometimes you just needed a slimmer coil. After due consideration, I decided to send the whole thing back to him for reassembly. I've learnt that sometimes the secret of DIY is knowing when not to!

The reassembled dynamo arrived back a week later and was perfect. Time to offer it onto the engine. I fed it through the dynamo clamp OK and with its new cork seal in place it fit nicely up against the back of the inner timing cover. Time to go into the draw and pull out the dynamo drive sprockets. For those of you you are following this blog, you may recall that on my 1st December blog I said that the eagle eyed BSA experts would notice that something was missing from the inner timing cover picture. It was at this point that I found it. Laying in the draw was a strange steel bush with two holes in it and a large flange. I had no idea what it was, but it looked important. All sorts of warning bells were ringing, had I got to strip the whole engine again?. I worked my way through the parts book until I found it. It's called the camshaft oil breather and it fits on top of the cork pad on the end of the camshaft, located by the peg that sticks through the cork pad and through the inner timing cover from the inside.

This meant removing the inner timing cover again along with the oil pump and tacho drive and of course a new gasket. The other thing that happens as you remove the inner cover is that the centre timing gear comes off with it and the valve timing is lost. So I reset the valve timing fitted the oil breather, checked the end float, fitted a new gasket and reassembled.

Now at last I can fit the dynamo sprockets, along with another cork spacer behind the big one and then the drive chain around the two sprockets. It was then simply a case of rotating the dynamo to tighten the chain. A hard press on the dynamo to make sure that the cork gasket seals against the back of the inner timing cover and tighten the dynamo clamp. Now the oil pump and tacho drive can be refitted and at last the outer timing cover fitted.

This final picture shows the rebuild a little further on with the exhausts fitted, but I'll cover that on another blog.

For those of you who follow this blog, you will have noticed that there has been a gap of about 6 weeks since the last one. This was due to the decision to buy a box trailer to transport my bikes in to shows. The huge amount of work necessary to make the box trailer usable accounted for the missing progress on the A10 and will be featured in another blog later.




I would love to read your comments on this blog. If you would like to make some please click "Subscribe to: Post Comments (Atom)" at the bottom of this page. If you would like to be automatically informed when a new episode is posted then please tick the "Join this site" box at the bottom of the page. Thanks for reading. Kevin

 Copyright K. Hopcroft  17.02.13 All rights reserved
 You can contact me on: hopcroftscoot@gmail.com

My Other Blogs:

1961 Ariel Arrow Super Sport Motorcycle :
http://60sclassicmotorbikes.blogspot.co.uk/2014/01/1961-aerial-golden-arrow-restoration.html

Miniature Land Rover Defender:
http://miniaturelandrover.blogspot.co.uk/2016/02/1-miniature-land-rover-defender-idea.html?view=timeslide

1971 VW Karman Ghia Convertible Car:
http://karmannghiarestoration.blogspot.co.uk/2017/03/1-karmann-ghia-retoration-project.html

Motorcycle Trailers / Caravans:
http://motorcycletrailersandcaravans.blogspot.co.uk/2018/01/1-motorcycle-trailers-problem.html